Repair of a Classic Chair

by scottdesignworks in Workshop > Furniture

823 Views, 7 Favorites, 0 Comments

Repair of a Classic Chair

65EB7F51-A65A-4CE5-9857-289E4902882C_1_105_c.jpeg

One of our Knoll 1601 stacking chairs by Don Albinson (1964) developed a crack in the polypropylene back. Almost nothing sticks to polypropylene, and I knew that attempting to weld it would almost certainly look horrible. So I decided to make a repair embellishment rather than try to fix it invisibly.

​Plan the Repair.

E1D8B6B9-5BA7-4354-9B16-D6C9FA099B38_1_105_c.jpeg
36487311-1480-465C-9D1E-7D3AB6EBBBD3_1_105_c.jpeg
815A842D-A89B-4316-953E-A62C876611C8_1_105_c.jpeg
06463A95-37CA-440A-89AB-A591D84A17F8_1_105_c.jpeg

I wanted to use leather laces to stitch the back together again. So I went to my leather lace bag and picked a few different types that I guessed were long enough. Then I laid them on the chair to get an idea how they would look.

​Lay Out the Spacing.

CCD2A9F9-90E2-49C0-BD58-27D38CBB483B_1_105_c.jpeg
656FE03F-9216-4CFE-88DE-37C7741F0CA4_1_105_c.jpeg
0FFA82E1-5F80-4355-8C48-A28DE6F12D55_1_105_c.jpeg
CA98D5D4-1567-46C7-9DE8-5C26086BFFA4_1_105_c.jpeg

The break measured 270mm long which made me think to divide by nine and get an even 30mm spacing. I used white tape to mark this out. 12mm on each side of the crack felt like the right distance for the holes.

​Make the Holes.

741D2BC5-BB90-40B2-90A1-63D02757AD88_1_105_c.jpeg
9465CE66-179D-421A-BC9B-11DF02E0C59E_1_105_c.jpeg
F81BC50D-19AA-4140-B27D-86AB43C17605_1_105_c.jpeg
13A85D48-5CB1-4C50-B0B6-E0E06B8B452D_1_105_c.jpeg
92C55E86-B1D9-4B7A-AD29-AFAA7AE041DF_1_105_c.jpeg

I used an awl to dimple the marks for drilling. This keeps the drill bit from wandering off the marks. The leather I decided to use fit nicely through a 5/32” hole. I started with a smaller bit and then enlarged to 5/32”. This makes any inaccuracy smaller.

Lace It Up.

819009C6-0EB2-42EE-8036-561D3D177E24_1_105_c.jpeg
9C06FF1B-8907-44D0-8ECF-194376C1CCAD_1_105_c.jpeg
157209FA-DEB1-424D-B233-E195AF6DB95C_1_105_c.jpeg
2EB3AB60-ACDA-4659-A203-F8E8152E8A2B_1_105_c.jpeg
A35686A5-0253-47D6-B08E-8EB888377F45_1_105_c.jpeg
84643E62-740B-4076-899A-130B430E3E06_1_201_a.jpeg
60FF4BE5-5E2D-455C-BD96-05AADC1ACD22_1_105_c.jpeg

I guessed that the top would take the most stress so I started there. That way the knot would be at the bottom where there would be less stress. I pulled even amounts of the lace through the top two holes and then made the first X. Then I crossed the laces on the back side and came out the next pair of holes. Continued to the bottom. Finished with a snug square knot.

And Done.

5463564E-D0D4-453F-BDE5-B7CF8D91988A_1_105_c.jpeg
23375711-0B22-4E5E-8AEE-A798BE095715_1_105_c.jpeg

The ends are left long to complete the statement that repairs done well have nothing to hide.